Davey
Rock Stacker
Hoping someone else has had and resolved this issue. My buddy installed a brand new standard rotation Titan 21t motor into his Bomber.
He’s running the stock AE-5 ESC, a brand new Spektrum DX5C as well as the new SR415 Rx.
When he follows the bind procedures, the Rx binds up no prob and the servo works fine, but the second it binds, the motor goes full throttle.
We’ve tried reversing the throttle in the settings, lowering the throttle rate to see if the motor would spin at a lower speed (no change), and have checked the plugs and ports and everything looks good.
Any ideas? He says the ESC was still operational when he put the rig away last.
It seems like the failsafe setting is defaulting to something other than zero/neutral during the bind process, or maybe this is just simple wiring issue, or worst case, a fault in the ESC...
Any ideas? Thanks -Mark
Sent from my iPad using Tapatalk
He’s running the stock AE-5 ESC, a brand new Spektrum DX5C as well as the new SR415 Rx.
When he follows the bind procedures, the Rx binds up no prob and the servo works fine, but the second it binds, the motor goes full throttle.
We’ve tried reversing the throttle in the settings, lowering the throttle rate to see if the motor would spin at a lower speed (no change), and have checked the plugs and ports and everything looks good.
Any ideas? He says the ESC was still operational when he put the rig away last.
It seems like the failsafe setting is defaulting to something other than zero/neutral during the bind process, or maybe this is just simple wiring issue, or worst case, a fault in the ESC...
Any ideas? Thanks -Mark
Sent from my iPad using Tapatalk